ARGG工艺重油催化裂化装置节能降耗的研究
本文选题:节能降耗 切入点:重油催化裂化 出处:《东北石油大学》2017年硕士论文 论文类型:学位论文
【摘要】:目前,我国催化裂化装置的能耗非常高,已经占炼油工业总能耗的30%以上,采取有效的技术改造方法降低催化裂化装置能耗,对炼油企业来说,降低能耗是至关重要的。本论文针对大庆炼化公司1.8Mt/aARGG装置,采用北京石油化工科学研究院开发的ARGG专利技术,主要包括反应-再生系统、分馏系统、稳定系统、干气和液态烃及汽油脱硫系统、烟气余热回收系统。于2009年9月检修期间实施MIP-CGP技术改造,使稳定汽油烯烃含量降低10个单位以上,产品分布和油品质量得到有效提高,装置能耗在一定范围内发生了明显降低的现象,根据工业标定数据,分析了装置能耗高的主要原因为:油浆管线和换热器管束流速低,系统易结焦,内提升管曾经被磨穿,胺液再生塔经常波动,胺液再生质量差,外取热本体有热点,制约装置长周期运行的瓶颈因素等。经过科研人员和检修人员的扎实工作,通过对烟气轮机、反应汽提段、进料喷嘴、余锅系统、汽油精制等系统进行了一系列的技术改造,实现装置催化剂单耗降低;油浆外甩量降低;降低了装置非计划停工风险。催化剂单耗下降每年可节约催化剂690.20吨,催化剂不含税单价18325.43元/t,每年节约辅助材料费用1265万元。沉降器旋分效率提高,油浆固体物含量下降,可将油浆产率控制在合理范围内(4.5%),目的产品收率提高,ARGG装置催化裂化汽柴油产量增加。
[Abstract]:At present, the energy consumption of FCC units in China is very high, accounting for more than 30% of the total energy consumption in the refining industry. It is very important to reduce energy consumption. In this paper, the ARGG patent technology developed by Beijing Petrochemical Research Institute is adopted for the 1.8 Mt / a ARGG plant of Daqing Refinery and Chemical Company, which mainly includes reaction-regeneration system, fractionation system, stabilization system, etc. Dry gas, liquid hydrocarbon and gasoline desulphurization system, flue gas waste heat recovery system. During the maintenance period in September 2009, MIP-CGP technology was carried out to reduce the olefin content of stable gasoline by more than 10 units, and the product distribution and oil product quality were effectively improved. According to the industrial calibration data, the main reasons for the high energy consumption of the plant are as follows: the flow rate of slurry pipeline and heat exchanger tube bundle is low, the system is easily coked, and the inner riser pipe has been worn through. The regeneration tower of amine liquid often fluctuates, the regeneration quality of amine liquid is poor, there are hot spots in the external heat extraction body, the bottleneck factors that restrict the long period operation of the device, etc. Through the solid work of the scientific research personnel and the maintenance personnel, through the flue gas turbine, the reaction stripping section, A series of technical revamping have been carried out in the feed nozzle, residual pot system and gasoline refining system to reduce the unit consumption of catalyst and the quantity of oil slurry. The reduction of unit consumption of catalyst can save 690.20 tons of catalyst per year, the unit price of catalyst is 18325.43 yuan / t without tax, and the cost of auxiliary material is 12.65 million yuan per year. The slurry yield can be controlled within a reasonable range of 4.5%, and the yield of the product can be increased by increasing the output of FCC gasoline and diesel oil in the ARGG unit.
【学位授予单位】:东北石油大学
【学位级别】:硕士
【学位授予年份】:2017
【分类号】:TE966;X742
【参考文献】
相关期刊论文 前10条
1 靳满满;田文德;张俊梅;;FCCU反再系统异常工况的安全分析[J];化工学报;2015年09期
2 李全善;李大字;曹柳林;;Modeling and optimum operating conditions for FCCU using artificial neural network[J];Journal of Central South University;2015年04期
3 张宇;杨进华;;浅谈催化裂化技术进展[J];广州化工;2013年08期
4 刘为民;孙国刚;胡敏;;催化裂化装置反应系统防结焦技术分析[J];炼油技术与工程;2012年06期
5 丁海中;栗文波;张洪军;倪胜发;;多产丙烯MIP技术在ARGG装置上的工业应用[J];石油炼制与化工;2011年10期
6 张显梅;;大庆炼化公司一套ARGG装置节能优化研究[J];化学工程师;2011年04期
7 刘学丽;陈跃军;;ARGG催化裂化装置辅助燃烧室存在的问题及解决方式[J];化工时刊;2011年03期
8 董庆;孙长波;;催化汽油精制新工艺的应用[J];化工科技市场;2009年03期
9 钱伯章;朱建芳;;低硫和超低硫汽油生产技术进展[J];天然气与石油;2008年02期
10 曾光乐;颜刚;潘罗其;顾湘兴;;ARGG装置技术改造及其效果[J];石油炼制与化工;2005年07期
,本文编号:1580675
本文链接:https://www.wllwen.com/shengtaihuanjingbaohulunwen/1580675.html