乳化液自动配比系统设计与优化
[Abstract]:Emulsion is regarded as the blood of underground support equipment and plays an important role in coal mine. The concentration of emulsion is the key factor affecting its performance, so it is necessary to control the concentration of emulsion accurately. The traditional emulsion manual and mechanical proportioning methods have been gradually eliminated because of their low precision and complicated operation. The automatic liquid distribution system mainly consists of two cylinder fixed ratio distribution system, the self-powered automatic matching system, the single-chip microcomputer control liquid distribution system and the PLC control liquid distribution system. Due to the lack of sensors, the system can not monitor the concentration of the system, while the automatic matching system can not guarantee the precision because of the underground wind pressure, the water pressure is unstable and the matching precision can not be guaranteed. The automatic liquid distribution system controlled by single chip microcomputer is mostly open-loop control, and the automatic liquid distribution system controlled by PLC is designed without the direct measurement of concentration sensor because the concentration sensor is easily affected by pollution in the process of use. The emulsion concentration is indirectly measured by the liquid level sensor. In fact, after the emulsion is fully mixed, the concentration sensor controls the accuracy of the system emulsion concentration much higher than the liquid level sensor under the condition of cleaning. Therefore, the improvement of automatic liquid distribution system needs to solve the problems of sufficient mixing of emulsion and contamination of concentration sensor. Based on the above problems, this paper has done the following research on the emulsion automatic proportioning system. First of all, the whole liquid distribution device is designed. The liquid distribution device integrates the emulsion tank and the emulsified oil tank, and for the sake of overall beauty, all kinds of actuators and sensors are embedded in the liquid dispensing device. All kinds of devices are connected to the junction box through the steel pipe inside the box. The whole structure of the distribution device is compact, simple and beautiful. At the same time, the wall thickness of the liquid distribution device is optimized, which makes the box body lightweight on the basis of satisfying the operating conditions, saves the cost and reduces the labor quantity of the underground workers. Then, the mixing time and energy consumption of the four straight blade turbine agitator, the 45 掳disk turbine agitator and the open 45 掳turbine agitator are compared by numerical simulation of the agitator, which plays a key role in the emulsion mixing, and the energy consumption is compared between the four straight blade agitators, the disk 45 掳turbine agitators and the open 45 掳turbine agitators. The results show that under the action of open 45 掳turbine agitator, the turbulence intensity in the liquid tank is the most uniform, the mixing completion time is the shortest and the mixing energy consumption is the least. At the same time, the effect of different installation heights of agitator on the emulsion mixing is analyzed numerically. When the blade height is 250mm, the whole emulsion mixing takes the shortest time. Secondly, the clogging problem of the concentration sensor is explored. The different installation positions and the different opening forms of the box block plate are not enough to wash the concentration sensor under the shear action of the agitator. Therefore, it is necessary to set up a washing device to clean the sensor. By comparing the axial velocity distribution of different nozzles and the dynamic pressure and impact force of the sensor wall, it is concluded that the wall dynamic pressure and impact force formed by the angular nozzle is the largest. When the inlet diameter is 8 mm, the contraction angle 伪 is 13 掳, the outlet diameter is 4 mm, the outlet diffusion angle 尾 is 20 掳and the inlet pressure is 3MPa, a good washing effect is obtained for the concentration sensor. Finally, the automatic control system based on the direct measurement of concentration sensor is designed, and the corresponding program and picture configuration are completed. The system has been tested on the ground and proved to be effective in underground operation.
【学位授予单位】:太原理工大学
【学位级别】:硕士
【学位授予年份】:2017
【分类号】:TD350.4
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